Please use this identifier to cite or link to this item: https://hdl.handle.net/11147/3419
Full metadata record
DC FieldValueLanguage
dc.contributor.advisorGünaydın, Hüsnü Muraten
dc.contributor.authorÇuğ, Özlem-
dc.date.accessioned2014-07-22T13:51:30Z-
dc.date.available2014-07-22T13:51:30Z-
dc.date.issued2006en
dc.identifier.urihttp://hdl.handle.net/11147/3419-
dc.descriptionThesis (Master)--Izmir Institute of Technology, Industrial Design, Izmir, 2006en
dc.descriptionIncludes bibliographical references (leaves: 83-84)en
dc.descriptionText in English; Abstract: Turkish and Englishen
dc.descriptionx, 84 leavesen
dc.description.abstractThis thesis investigates .Manufacturing design for productivity. surveying a case study of an assembly line for air conditioning control panels. The main aim is to investigate the possibilities of operational improvement on the production time in a cost-effective manner. The specific objective of this study is to investigate the relationship between manufacturing design and productivity issues. In order to achieve the objective of this study, a methodology has been developed. First a thorough literature survey is conducted. The use of methods engineering in the factory system is explained, then the relationships between analytical techniques of methods engineering are discussed. Then examples related to subject are investigated. Later on, an assembly line is selected as the case study. An ex-assembly is redesigned by using the concepts of methods engineering. Then both cases are analyzed and discussed in terms of their output capacity and manufacturing time. After the analysis of MTM for redesigned assembly line it is observed that we can reduce production cycle time 20 % at the end of this study. And this development project has been chosen for investment. At the end of this project, we increased the production quantity from 600 pcs. to 800 pcs. Because efficiency of workers have increased with the redesigned assembly line, production of the goods of quantity increased 13 % more than originally calculated. The new assembly line is reduce the operators waiting time and increases their efficiency. The ex-assembly line was covering 13,5m² square it reduce to 3,6 m². Finally, because of efficiency and productivity increase of this study, totally we observed 33 % production increase for the same period of time. By the standardization and the elimination of the operations, and reducing the labor cost the factory could increase its competitive strength.en
dc.language.isoenen_US
dc.publisherIzmir Institute of Technologyen
dc.rightsinfo:eu-repo/semantics/openAccessen_US
dc.subject.lccT58.8 .C96 2006en
dc.subject.lcshIndustrial productivityen
dc.subject.lcshDesign, Industrialen
dc.title'Manufacturing design for productivity' :optimization of assembly line for air conditioning control panelsen_US
dc.typeMaster Thesisen_US
dc.institutionauthorÇuğ, Özlem-
dc.departmentThesis (Master)--İzmir Institute of Technology, Industrial Designen_US
dc.relation.publicationcategoryTezen_US
item.openairetypeMaster Thesis-
item.openairecristypehttp://purl.org/coar/resource_type/c_18cf-
item.fulltextWith Fulltext-
item.languageiso639-1en-
item.cerifentitytypePublications-
item.grantfulltextopen-
Appears in Collections:Master Degree / Yüksek Lisans Tezleri
Files in This Item:
File Description SizeFormat 
T000559.pdfMasterThesis1.62 MBAdobe PDFThumbnail
View/Open
Show simple item record



CORE Recommender

Page view(s)

112
checked on Mar 25, 2024

Download(s)

148
checked on Mar 25, 2024

Google ScholarTM

Check





Items in GCRIS Repository are protected by copyright, with all rights reserved, unless otherwise indicated.